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Old 04-10-2007, 07:08 AM   #12
Randy99
 
Join Date: Nov 2006
Posts: 37
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JonJZ...

50-75 HP I'd venture to guess as the difference (back-up motor hasn't been dynoed in years, nor freshend up lol)...if there were some sort of vaccum leak in the fuel system or at the intake like you previously spoke about don't you think I would have seen a rise in water temperature?...I know anytime in the passed when i was fighting a lean condition or had any type of leak (intake or exhaust) it was noticable on the gauges...the motor would pick up about 10 degrees (h2o temp) ...when my motor went temps were all still in perfect operating order...motor made that flat sound, stumbled abit, water and oil temp spike, oil pressure and fuel pressure dropped, and then she made a lotta smoke...the biggest mystery is the size of the hole in piston #6...lean conditons on a SBC usually lead to a melted piston in #3 0r 5, no?

Thanks for your input Jon! I'm always looking for someone else who could lead me to an answer.

P.S...only thing different was the fuel pump and carb...motor builder took the carb that was on the motor when it blew up to "research"...fuel pump also stayed on the other motor...2 possible issues but i highly doubt it
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Previously owned: 91 Firebird, LO3...headers, !cat!, dynomax bullet, edlebrock performer intake, 3.73's, LCA's, Panhard, BFG's...mid 14's
93 T/A, CAI, Cat-Back, LCA's, Panhard, Hoosier QTP's...13.60's all day long, Bracket Beast

New Toys - 2006 and 2007 LE Prototype chassis
358 ci SBC, 12:1 by Bitner Automotive
358 ci SBC, 10:1 Vortec, built by 2 hackers in tool-shed

Last edited by Randy99; 04-10-2007 at 07:14 AM. Reason: added information, also typo
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