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Old 02-24-2018, 06:49 AM   #451
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Originally Posted by Blackbirdws6 View Post
Little squirt of WD40 and push them from the top vs pulling from the bottom.
Thank you Sir.
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97' Z28, M6 w/ golen engines 396 Lt1, rpm transmission level 6 t56, moser 12 bolt eaton posi w/ 4.11 gears, Hooker super comp long tube headers ory-pipe, slp loudmouth 1 .Full BMR suspension, Bilstein shocks. Torqhead 24x conversion.
02' SS, M6 BMR lowering springs, adj. pan-hard bar, Bilstein shocks. Lt1 front end conversion. Ford 9"
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Old 02-26-2018, 05:39 PM   #452
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So if anyone knows of a cliff I'd like to throw this car off of it. Decided to take it out for a drive today before I left for vacation and it stalls. Defiantly a tune issue...just tired of this. 5k spent on and a verighty of things done. Yes it made more hp but come on. It's going back to ttp, when I get back, and I don't want it back till it's fixed for good.

It's a cold start problem. But when I give it gas and let off the clutch and give it gas, it falls on its face now.
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97' Z28, M6 w/ golen engines 396 Lt1, rpm transmission level 6 t56, moser 12 bolt eaton posi w/ 4.11 gears, Hooker super comp long tube headers ory-pipe, slp loudmouth 1 .Full BMR suspension, Bilstein shocks. Torqhead 24x conversion.
02' SS, M6 BMR lowering springs, adj. pan-hard bar, Bilstein shocks. Lt1 front end conversion. Ford 9"

Last edited by bigz28man; 02-26-2018 at 05:43 PM.
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Old 02-26-2018, 07:51 PM   #453
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Ugh that sucks. The good part is you know what it is and how to get it resolved. Hopefully TTP will get it squared away with some more tuning. This is one of those skills I hope to improve upon.
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Old 02-28-2018, 10:36 AM   #454
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Drag it to TTP and then drag Matt out to fix it.

You paid for a tune, and he did not deliver, don't relent.
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repo bigals turd gen and part it out to a loving home
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Old 02-28-2018, 01:02 PM   #455
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Drag it to TTP and then drag Matt out to fix it.

You paid for a tune, and he did not deliver, don't relent.
I just don't get it the week I get it back (3 weeks ago today) it's breaking the tires loose going into 4th gear to this. What I have found is it got a "ticking" burn your eyes pre 02 exhaust leak. I feel and have pin pointed it to that slip joint hooker headers have. I'm done with these headers, they have a 4" band clamp from 3 years ago. Kooks long tubes and y-pipe have been ordered and getting ceramic coated. Should be 4 weeks. I just don't see this exhaust leak was not seen through live info.

Now i sit and ponder obout this opti spark sitting in my garage. Yes it did through opti codes but it needs to be tested on what failed. My stomach is turning slightly thinking this opti spark is fine
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97' Z28, M6 w/ golen engines 396 Lt1, rpm transmission level 6 t56, moser 12 bolt eaton posi w/ 4.11 gears, Hooker super comp long tube headers ory-pipe, slp loudmouth 1 .Full BMR suspension, Bilstein shocks. Torqhead 24x conversion.
02' SS, M6 BMR lowering springs, adj. pan-hard bar, Bilstein shocks. Lt1 front end conversion. Ford 9"
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Old 02-28-2018, 05:56 PM   #456
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Sounds like you have a bigger problem than an exhaust leak.
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Old 02-28-2018, 06:45 PM   #457
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Sounds like you have a bigger problem than an exhaust leak.
What comes to mind? Lifters? anyway to check without tearing motor apart? Just seems like that sound is down real low by that slip joont
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97' Z28, M6 w/ golen engines 396 Lt1, rpm transmission level 6 t56, moser 12 bolt eaton posi w/ 4.11 gears, Hooker super comp long tube headers ory-pipe, slp loudmouth 1 .Full BMR suspension, Bilstein shocks. Torqhead 24x conversion.
02' SS, M6 BMR lowering springs, adj. pan-hard bar, Bilstein shocks. Lt1 front end conversion. Ford 9"

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Old 03-01-2018, 10:50 AM   #458
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Could be as simple as a burnt coil wire, or burnt 02s
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repo bigals turd gen and part it out to a loving home
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Old 03-01-2018, 02:51 PM   #459
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I spoke with Doug over at east coast supercharger said he would take an hour and tell me what he thinks...what do you guys think?
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97' Z28, M6 w/ golen engines 396 Lt1, rpm transmission level 6 t56, moser 12 bolt eaton posi w/ 4.11 gears, Hooker super comp long tube headers ory-pipe, slp loudmouth 1 .Full BMR suspension, Bilstein shocks. Torqhead 24x conversion.
02' SS, M6 BMR lowering springs, adj. pan-hard bar, Bilstein shocks. Lt1 front end conversion. Ford 9"
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Old 03-01-2018, 03:22 PM   #460
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Have you spoke to anyone at TTP about your issues? Maybe they can help you since they just worked on the car.
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Old 03-01-2018, 03:22 PM   #461
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I spoke with Doug over at east coast supercharger said he would take an hour and tell me what he thinks...what do you guys think?
If TTP did the work, they should fix it.

Once you bring it elsewhere TTP will never agree to work on it
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repo bigals turd gen and part it out to a loving home
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Old 03-01-2018, 03:52 PM   #462
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Have you spoke to anyone at TTP about your issues? Maybe they can help you since they just worked on the car.
+1 rule of any contracting field, never take it to multiple people or have multiple companies look at the same problem. You'll never figure it out that way, or it'll cost 10x as much.
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Old 03-01-2018, 04:24 PM   #463
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I spoke to ttp the other day when the issue was accruing prior to me leaving. They did say bring it right over, when i get back. So next Thursday (1 week from today when I get home) we'll see whats up.
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97' Z28, M6 w/ golen engines 396 Lt1, rpm transmission level 6 t56, moser 12 bolt eaton posi w/ 4.11 gears, Hooker super comp long tube headers ory-pipe, slp loudmouth 1 .Full BMR suspension, Bilstein shocks. Torqhead 24x conversion.
02' SS, M6 BMR lowering springs, adj. pan-hard bar, Bilstein shocks. Lt1 front end conversion. Ford 9"
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Old 03-11-2018, 01:26 PM   #464
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Any Updates?
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Old 03-11-2018, 03:55 PM   #465
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Any Updates?
None Sir, I got back mid afternoon last Thursday and have been stuck working. spoke with Tom over there, it's going to go this Thursday. I hope its something stupid. I also developed that oil leak again from the rear of the oil pan. Trying to determine if it's the drain plug, oil pan seal, or rear main. Oil is dripping from the plug area onto cardboard. Insert photo of me bashing my head against wall.
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97' Z28, M6 w/ golen engines 396 Lt1, rpm transmission level 6 t56, moser 12 bolt eaton posi w/ 4.11 gears, Hooker super comp long tube headers ory-pipe, slp loudmouth 1 .Full BMR suspension, Bilstein shocks. Torqhead 24x conversion.
02' SS, M6 BMR lowering springs, adj. pan-hard bar, Bilstein shocks. Lt1 front end conversion. Ford 9"
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Old 03-14-2018, 03:57 PM   #466
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Got the car to ttp this morning. On the way there every time I get to a stop light, the rpms would drop as low as 600 then slowly climb back up to 1000. Usually its the opposite, I'd get to said stop light rpms would stay at about 1700 for a few seconds then drop to 1000.
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97' Z28, M6 w/ golen engines 396 Lt1, rpm transmission level 6 t56, moser 12 bolt eaton posi w/ 4.11 gears, Hooker super comp long tube headers ory-pipe, slp loudmouth 1 .Full BMR suspension, Bilstein shocks. Torqhead 24x conversion.
02' SS, M6 BMR lowering springs, adj. pan-hard bar, Bilstein shocks. Lt1 front end conversion. Ford 9"
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Old 03-15-2018, 06:58 AM   #467
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Good you got it there. Now let's hope they figure it out with little trouble.
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Old 03-20-2018, 01:43 PM   #468
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So ttp says there is nothing wrong with the car. Ummm What? After mother nature gets done with her nonsense, I'll be picking the car and bringing it home.
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97' Z28, M6 w/ golen engines 396 Lt1, rpm transmission level 6 t56, moser 12 bolt eaton posi w/ 4.11 gears, Hooker super comp long tube headers ory-pipe, slp loudmouth 1 .Full BMR suspension, Bilstein shocks. Torqhead 24x conversion.
02' SS, M6 BMR lowering springs, adj. pan-hard bar, Bilstein shocks. Lt1 front end conversion. Ford 9"
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Old 03-20-2018, 02:31 PM   #469
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So ttp says there is nothing wrong with the car. Ummm What? After mother nature gets done with her nonsense, I'll be picking the car and bringing it home.
Well thats more than a little bit frustrating. Do you think you can easily repeat the issue? If so, I'd suggest they put someone in the car with you to show them the problem.
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'24 Corvette Z06
17 Sierra 2500HD Dmax
81 Turbo TA
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Old 03-20-2018, 06:24 PM   #470
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So ttp says there is nothing wrong with the car. Ummm What? After mother nature gets done with her nonsense, I'll be picking the car and bringing it home.
Unless you want start from scratch some where else, just bite the bullet and be a pain in the ass to TTP.

Force them to show you that its not a tune issue.
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repo bigals turd gen and part it out to a loving home
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Old 03-20-2018, 07:23 PM   #471
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I don't know guys. I told them about the drop in idle approaching a stop, maybe the hesitation is just me. I'll talk more with them when I can get over there
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97' Z28, M6 w/ golen engines 396 Lt1, rpm transmission level 6 t56, moser 12 bolt eaton posi w/ 4.11 gears, Hooker super comp long tube headers ory-pipe, slp loudmouth 1 .Full BMR suspension, Bilstein shocks. Torqhead 24x conversion.
02' SS, M6 BMR lowering springs, adj. pan-hard bar, Bilstein shocks. Lt1 front end conversion. Ford 9"
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Old 03-21-2018, 09:47 AM   #472
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Old 03-21-2018, 12:47 PM   #473
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can you do any data logging on your own and show logs of the issue?
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and once i get PHB, what do i ajust it too?
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Old 03-21-2018, 01:49 PM   #474
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can you do any data logging on your own and show logs of the issue?
Or get a GoPro and take a video of the behavior.
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Old 03-21-2018, 04:06 PM   #475
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Spoke with Matt and expressed my frustration, they are keep the car through the weekend to log more miles on it and try to get it to duplicate this extremely low idle it had. Matt said he may add more timing down low. I don't have the ability to data log on my own.
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97' Z28, M6 w/ golen engines 396 Lt1, rpm transmission level 6 t56, moser 12 bolt eaton posi w/ 4.11 gears, Hooker super comp long tube headers ory-pipe, slp loudmouth 1 .Full BMR suspension, Bilstein shocks. Torqhead 24x conversion.
02' SS, M6 BMR lowering springs, adj. pan-hard bar, Bilstein shocks. Lt1 front end conversion. Ford 9"
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